Tag Archives: floor patching & leveling (H3-40)

2015/11/10 (T) A Rainy Day

I checked the TV weather station before I turned off the lights last night.  Rain covered most of Indiana and Ohio and was moving northeast.  We were going to get clipped by the western edge of the moisture but the heaviest rain was forecast to pass to our south and east.

Linda planned to go into the bakery today and had her alarm set for 5:45 AM.  It went off and I woke her up enough to shut it off and go back to sleep.  Around 6 AM we both received e-mails on our iPads and phones, a sure sign that we had lost power to the house.  I was awake at this point but stayed in bed until 6:45.  I was not falling back asleep, so I put on my robe and made coffee.  I finished up the Kenya AA, which is not decaffeinated, figuring we could both use the boost this morning.

While the coffee was brewing I cleaned the cats’ litter tray and checked my e-mail.  I had a reply from Bill Tharpe which decided for me that I would be going to Indiana on Friday.  I also had replies from the two Mitch’s who had contacted me as about articles I wrote in Bus Conversion Magazine and replied to both of those.  I edited the e-mail with the minutes of Sunday’s SLAARC meeting and forwarded it on to the club officers.  An e-mail from Gary at BCM indicated that they still needed a photo of Byron and Betty Pigg for the December featured bus article, so I replied and cc:d Byron.  Writing for BCM is sometimes a lot of work, but it’s a hobby for and I enjoy it so I do not mind.

It was wet outside and still raining lightly, a perfect day to sit by the fireplace in a robe and drink hot coffee.  Phil was hoping to return today with a load of screened topsoil and get it placed and graded along the edges of the driveway but said it would depend on the weather.  Once the topsoil is taken care of he will grade the driveway with his bulldozer and make sure the 40 foot long parking area is as flat and level as possible.

Linda finally got up at 8:30 and was starting to get dressed to go to the bakery when I suggested she stay home, rest, and get well.  She was immediately OK with that idea, put on her robe, and took her iPad to the living room to enjoy the warmth of the fireplace and some hot coffee.  I finished up my draft blog post for yesterday, e-mailed it to myself, and started this one.  I really cannot afford to lose a whole day of work on the bus but this is the kind of day where we like to just sit and do quiet things, or even nothing at all.  We finally finished our coffee, got dressed, and had a light breakfast at 10 AM.

Taking care of Madeline for three days and nights took a lot of Linda’s mental and physical energy and her cold took what was left.  She headed back to bed and I got my thoughts organized relative to working in the bus.  I talked to Jarel yesterday and found out that it would cost $50 to have a sheet of 1/4″ Baltic Birch plywood delivered to his shop because he did not have a regular delivery scheduled and the $50 cost of the 60″x 60″ sheet would not meet the minimum cost for free delivery.  I did not need the piece of plywood badly enough to pay a 100% surcharge to get it so that idea was off the table until next year.

My goal for today was to get a piece of SurePly underlayment cut and installed on the passenger seat platform.  Before I even started on the piece I had to resolve what to do about the four carriage bolts that are used to mount the base.  One of the four bolts has some messed up threads but I have a tap and die set and might be able to clean them up.  However, I am adding the thickness of the underlayment and floor tile plus a washer to what was there before so I wanted to use a longer bolt.  I already knew that Lowe’s and O’Reilly’s did not have what I needed and I presumed that The Home Depot did not either.

I finally went to Howell Hardware and had a good QSO with Steve (N8AR) on the drive there.  As I had been told they had a very good selection of hardware, by the piece, but they did not have fine thread carriage bolts in the 1/2″ size I needed.  I bought four of the 2″ long coarse thread bolts, four flat washers, four lock washers, and four nuts.  I also picked up a large washer to match the other three I already had for securing the central mounting stud along with two nylon washers.  That trip took over an hour out of my day before I even got started on my main task.

It took me several hours and many trips back and forth between the bus and the shop (in the garage) to get the piece of underlayment to fit just right.  I made one small mistake but the piece was large enough and complicated enough that I did not want to take the time or material to remake it.  Before I could install it I needed to get the outside end of the floor patch secured.  Yesterday I tried to screw that end to the material underneath it but the screw would not penetrate.  I scratched my head for quite a while until it occurred to me that I could use a small angle bracket attached to the vertical wood wiring chase in the forward outside corner.  I had limited access to that area, and it took me multiple attempts before I finally got the screw in, but I did.  Securing the bracket to the floor patch was a lot easier.

After securing the end of the patch I realized that the area between the front mounting channel and vertical front of the platform was slightly concave.  It was not a big dip but it was big enough that it needed to be patched.  Floor patching compound was the last thing I wanted to deal with today but it turned out to be just that, because once I applied it it had to dry for hours.  It was heavily overcast all day and my mood was correspondingly suppressed so I felt like I was doing everything in slow motion.  Based on the fact that I did not even get the piece of underlayment installed perhaps I was.

I try to keep an eye on the “house” batteries in the bus.  When I checked them this afternoon the reported voltage was higher than normal so I turned off the charger function on the Magnum 4024 to let the batteries rest and see where the voltage really was.  The DC draws on the battery bank were minimal.

I am finishing this post a couple of days later and no longer recall what Linda fixed for dinner but whatever it was I’m sure it was good.  After dinner we relaxed in the living room for a while, watched our Tuesday evening TV programs on the larger TV set in the basement recreation room, and then went to bed.

 

2015/11/09 (M) Clever Mouse

Madeline coughed quite a bit last night and we were up several times to check on her, so we did not have the best possible night’s sleep.  We got up to stay at 7:30 AM and Madeline got up about 15 minutes later.  I made our morning coffee while Madeline helped her grandma wash blueberries and make vegan blueberry pancakes.  We had a lovely breakfast with orange juice, pancakes with real maple syrup, and blueberries, raspberries, and bananas on the side.

I check the mouse traps in the pantry every morning.  A couple of days ago I found one of them broken with the food gone and some mouse poop left in its place.  The pantry doors had been left open overnight so I figured one of the cats had discovered the trap (we use live traps) and tossed it around until the door fell open and the mouse escaped.  I threw it away since it was broken.  This morning I discovered that the food in the other trap had been replaced by mouse poop but the trap was upright with the door closed and was not broken.  The pantry had been closed all night so I knew the cats had nothing to do with it.  Apparently we have a mouse that has figured out how to defeat the traps.  We are not going to set kill traps so we will have to see what else we can find.

We lingered in the living room for a while enjoying our coffee by the fireplace, listening to Madeline play (with) the organ, and watching her play with some of her toys.  She made her futon into a car and took her two “bunnies” for a ride.  By 9:30 AM I had finished my coffee and changed into my work clothes.  It was just below freezing when we got up this morning, but it was a bright, sunny day with no wind, so it would be a comfortable enough day for working on the bus once I turned up the thermostats and warmed up the interior a bit.

My focus today was to get the SurePly underlayment installed on the floor of the passenger seat platform and maybe the two walls.  I also wanted to get the outside wall panel trimmed off so it will fit around the tile and needed to build a new step with an open front, but I did not expect to get to those tasks today.  First up, however, was getting the small patch I worked on yesterday to fit better and be secure.

I trimmed both ends of the underside of the main patch and recut the side/support panel.  I trimmed the side panel several times before I was satisfied with the fit.  I used heavy-duty double-sided tape to hold the top patch and side panel to the metal structure underneath.  I used a 1-1/2″ stainless steel self-drilling wood screw to secure the top to the vertical piece of 3/4″ plywood that forms the face of the passenger seat platform, and a shorter screw to secure the side panel to the same piece of plywood.  I then attached a temporary plate of SurePly over the side panel to the edge of the top plate to hold the side in alignment with the top.

The metal under this patch is rounded leaving a small space between the top and side pieces where they meet.  The vertical plywood front face is also beveled leaving a void.  I used Door and Window Trim Spray Foam Insulation to fill these areas.  This foam has a lower expansion than most spray foam insulation.  I did not overfill the voids but put enough in that it expanded out past the edge.  I will trim it off flush tomorrow when it is cured.  The foam adheres to anything it touches and is rigid enough to be somewhat structural so it should stabilize and secure the patch.  Once I trim it and cover it with underlayment it should be good as new.

Madeline’s Aunt Meghan, who is also her buddy, came to visit and play with her today.  She arrived at noon and I took a break to visit and have lunch.  After lunch Madeline, Meghan, and Linda went to the Brighton Mill Pond Playscape and I resumed working on the bus.  They were gone for several hours.

Floor patching compound being applied to the co-pilot/navigator platform.

Floor patching compound being applied to the co-pilot/navigator platform.

Before I could put a layer of underlayment on the passenger seat platform I needed to use floor patching compound to fill in some low spots and create a smooth taper from the plywood to some metal edging.  But first I removed all of the screws that secure this edging and counter-bored the holes so the screw heads would be flush.  As often seems to happen when I am working on something like this some of the screws were rusted and I did not have appropriate replacements.  I then have to make a trip to Lowe’s, which is what I did, and bought a small quantity of three different size flathead wood screws.  I stopped at O’Reilly’s Auto Parts to see if they had the large metal or nylon washers that are used with the swivel base for the front chairs.  They didn’t, but once again suggested that I try Howell Hardware in downtown Howell.  I have received that suggestion from people at several different stores so guess I need to check the place out.

When I got back home I finished installing the new screws.  The floor patch compound takes a minimum of three to four hours to dry, sometimes much longer, but after two hours it was dry enough for me to use a sanding sponge to smooth out some ridges and feather some edges that needed it.  It was clear, however, that I wasn’t going to be able to accomplish what I set out to do today.  And so it goes; I need to do the work correctly which means doing all the things that need to be done in the order that they need to occur.  Everything takes time and things that have to dry, set, or cure do so on their own schedule, not mine.

Phil had shown up around 3 PM so I went out to chat briefly with him and then went inside to change clothes.  He had a partial load of topsoil left from a job earlier today and dumped it on the other side of the street by the 3rd driveway culvert.  He used his front loader to place it along the south side of the new pull-through driveway extension and moved the small pile from the west end of the property to the north side of the driveway.

I still had plenty of daylight and wanted to make some good use of my time so I started thinking ahead to the layout of the tile in the cockpit.  I measured various parts of the cockpit and although the number of square feet is small compared to the main floor the layout will be more difficult.  As with all tile layouts it needs to be “balanced” while avoiding small pieces.  Linda and I agreed that the pattern in the cockpit does not need to match the main floor, which is laid out diagonally, so that opens up options for how to lay out the tile.

The main landing is less than two tiles wide (front-to-back) so the best layout for that area is with a grout line dividing it in half, but that might not work well in the driver’s area.  The driver’s area presents the additional problem of a steering column, brake pedal/valve, an accelerator pedal with its electrical cable that goes through the floor.  The “holes” in the tile to accommodate these things have to be created using two notched pieces so they can be installed around the protrusions.  I also need holes for the seat base mounting bolts and power cable for the 6-way power base.  Those can be actual holes but I do not want grout lines to fall at the edges of the base.  I also have to be cognizant of the walls, which are getting tiled.  The distance along the face of the passenger seat platform is close to 65″.  The tiles are 16″ squares so four tiles with three 1/8th” grout spaces is only 64-3/8″.  See, it’s complicated.

The other thing I pondered and measured was the new step between the passenger seat platform and the main floor.  Again there are several parameters:  (1) We want the finished (tiled) height to split the distance from the tiled platform to the tiled main floor exactly in half; (2) we want the finished depth to be half the finished depth of the platform, and; (3) we want an open front so we can store shoes under the step.  The total rise will be just under 14″ so the step rise will be a little less than 7″.  Subtracting about an inch for wood and tile will leave a 6″ high space for shoes.  The platform is 29″ deep so splitting that in half results in two treads of 14-1/2″, plenty deep for shoe storage.  I considered having the step angle across the platform, being deeper by the driver seat and shallower by the passenger seat.  While it would add an element of aesthetic interest it would greatly complicate the construction without adding any practical utility, so I rejected that idea.

As I considered the construction of the new step I was also thinking about the fact that there is a hole in the front end of the passenger side HVAC duct.  The hole opens into the space behind the switch panel on the wall next to the passenger seat and just aft of the entry door but there is nowhere for the air to go from there.  The hole is easy to see but not easy to reach so I estimated it to be three inches in diameter which is approximately seven square inches in area.

One possibility is to install a 4″ diameter circular louvered duct in the switch panel.  It would be large enough in area, could be rotated to direct the flow in any desired direction, and has internal shutters that could be closed down to reduce or cut off the air flow.  The main downside is lack of space behind the panel but I could cut off the tube behind the locking tabs.  Another downside is that the cats sleep under the passenger chair while the bus is moving and the direct airflow might be uncomfortable and/or annoying for them.

Another possibility is to create a narrow duct along the back wall of the platform the same height as the new step and tie it in to the inside of the step, allowing the conditioned air to come out the open front.  That will involve a bit more woodworking and complicate the tile installation, but could be added later, so I will probably opt for the round louvered register for now, if I do anything.

When I was done pondering the HVAC possibilities I put the seat pedestals back on the landing, locked up the bus, and went inside to change clothes.  Meghan left while I was changing clothes so I did not get to say goodbye.  Apparently Linda thought I was taking a shower and would be a while.  Since we needed to get Madeline back to her house well before her bedtime we decided to head to Ann Arbor and have dinner there.  I deflated and rolled up her portable toddler bed while Linda and Madeline gathered up her clothes, books, toys, and other things.  I loaded the car while Linda got her dressed to travel.  I checked in with Phil to get a status update and let him know we were leaving.  We were on our way at 4:45 PM.

The drive down was OK as the really heavy traffic was headed north out of Ann Arbor.  We tried to keep Madeline awake by reviewing all the fun things she had done since she got to our house late Friday afternoon but we were not successful.  As I exited M-14 eastbound onto US-23 southbound I could see that traffic was stopped not far after the Plymouth Road exit so I left the highway and headed west on Plymouth Road to Huron Parkway.  From there I headed south, paralleling US-23 to the west.  At Washtenaw Avenue I turned east, and after a short distance turned left into the small shopping plaza where Elevation Burger was located.

I order a grilled cheese sandwich and Mandarin oranges for Madeline.  Linda and I had vegan burgers and fries and Linda shared her fries with Ms. M.  Madeline was slow to wake up but perked up when her food arrived.  That girl likes to eat!  🙂  After dinner we made the short trip to Madeline’s house and arrived at 6:30 PM.  Linda got Madeline into her pajamas while I brought all of the stuff in from the car and turned up the thermostat.

Madeline was wide awake and full of energy so she played with her kitchen toys and tools and had Grandma Linda read her four stories.  I dozed off for a little while and then spent some quality time with Gus the cat.  Gus loves people but tends to keep his distance from Madeline who is just a bit too energetic and enthusiastic for him.

Brendan and Shawna’s flight was due in to Metro Airport at 6:50 PM and he texted Linda at 6:51 that they had landed.  They were home before 8 PM and got to spend time with their very awake, excited, and active daughter.  We left at 8:30 and stopped at Biggby Coffee on Washtenaw Avenue.  Rain was moving into our area from the south but had not yet arrived and the drive home was uneventful.  We were home by 9:15 PM and headed straight to bed where we watched Scorpion and NCIS-LA.  Linda came down with a cold while Madeline was here and went to sleep as soon as NCIS was over.  I watched Travelscope on the Create channel and left the TV on while I worked on this post.  It was another long, busy day during which I made forward progress on the bus.

 

2015/08/25 (T) Turning The Corner

It got pleasantly cool overnight and with the bedroom doorwall open it made for nice sleeping conditions.  Between being up a bit late last night and not wanting to get out from under the warm covers we slept in a few minutes longer than usual.  I put on my sweats, which I find very comfortable on a cool (or cold) morning, and made a pot of Costa Rican decaf coffee.  We had our usual granola for breakfast, took a few minutes to enjoy our coffee in the living room without our cats, who were off somewhere and probably up to no good, and then got to work.

In order to install the new seats in September we need to have the desk installed and in order to install the desk we need to have the floor installed and in order to install the floor we need to have the underlayment installed and in order to install the underlayment we need to have several things done.  First and foremost was finishing the patching and leveling of the subfloor, so that was my first task today.  While I pursued that Linda continued working on cleaning and waxing the walnut drawer fronts.  Given the limited work surface in the garage Linda can only work on three to six drawer fronts at a time depending on their size.  When she reached a stopping point with those and started working on the woodwork in the bedroom.

I have spent the last week patching, skimcoating, and sanding the entire area where the old tile was installed which I estimate to be about 80 square feet.  I went over it one more time this morning with 80 grit sandpaper on the orbital sander.  The sander has an integral dust collection bag so it did not get the coach too dusty.  I was satisfied with most of the job but still had some unevenness along the edges by the walls and especially in the toe kick spaces extending out about three inches from the cabinet bases.  That is because I did not get the last skimcoat as smooth as I needed to in those areas and the orbital sander cannot reach them.

 

I figured I would need to do one more application of floor leveling compound but did not want to open the second bag of mix for such a small job.  I decided to go the Lowe’s and buy a small pail of pre-mixed floor patching compound and the 3/4″ #8-32 machine screws we needed to install the new handles.  While I was there I noticed that they had 50 grit hook and loop sandpaper triangles designed to fit our Porter-Cable oscillating saw.  I was aware that we had a sanding pad attachment for the tool but had not considered using it until I saw the 50 grit paper.  I bought a pack and picked up some 120 grit as well.  I would also have bought 80 grit but they were out.  I had to go to The Home Depot for the machine screws as I wanted the same brass ones we had already purchased.

Back at the bus I decided to try sanding out the imperfections rather than filling them in with another round of patching and sanding.  I was, admittedly, tired of this phase of the work and anxious to be done with it so I could move on to next step.  August is slipping away and I am very aware of the date.  I was also not keen on creating more sanding dust inside the coach.

I don’t know why I did not try this tool sooner.  The design of the tool and shape of the sanding pad allowed me to work in the all of the areas the orbital sander could not reach and it worked very well with the 50 grit sandpaper.  The circular air sander can also reach these areas, and was the right tool for grinding down the old thinset and mastic, but the oscillating tool was the right one for this final smoothing.

When I thought I was done I vacuumed the floor and used the Revel Damp Mop to pick up any residual dust.  We then went inside to have lunch while the floor dried.  Linda heated up a can of Amy’s vegetable soup, made roll-up sandwiches, and served fresh black grapes and plums.  It beats fast food hands down.

After lunch I inspected the floor carefully and decided that the patching and leveling was done.  Although it was one task out of many, and there was no fanfare attached to the moment, I was very much aware that we had finally turned the corner.  We still have some minor disassembly to do, but from this point forward most of our tasks will involve putting the interior back together and installing new things.  All things being equal (which they never are) the building work should be more fun than the deconstruction work.

The major exception is the wallpaper.  We still need to remove the old paper, much of which is stained from old water leaks, and install the new paper, which Linda will be ordering tomorrow from Delux Drapery and Shades in Ann Arbor.  The critical pieces are the ones that go behind the desk and the built-in sofa.  Most of the rest of it can be finished later but we would prefer to have it all done by September 12th if possible.  The more stuff that gets installed the more awkward it will be to work on the walls.

With the floor leveling done the next impediment to installing the underlayment was getting the refrigerator out of the living room and into its alcove.  That, however, required three other things to be done.  First I needed to replace the electrical outlet with a recessed one.  Second, we needed to build up the base of the alcove and finally, we needed to install the pantry as we cannot get to the slides to mount them to the side of the alcove with the refrigerator in place.

The electrical outlet only took a few minutes to change.  With Linda’s help I used the template I made last Thursday to cut the base pieces from the 4′ x 8′ sheet of 3/4″ plywood we bought on Tuesday.  The bottom piece was the full width of the refrigerator alcove (34″ wide at the front and 33.75″ wide at the back) and 25.75″ deep.  We set it in place, checked the front setback, and screwed it to the subfloor.  The next piece was the same width as the first but 1/2″ deeper (26.25″).  We set it in place on top of the first piece and made sure the front edges were flush with the back edge extending 1/2″ farther back.  I used longer screws to go all the way through both pieces into the subfloor.

I was not happy with the way my circular saw blade was cutting and a few raindrops gave us an excuse to take a break.  We were working just outside the small garage bay and moved everything into the garage to keep it from getting wet.  I went to Lowe’s and bought a new 7.25″ blade with 60 teeth, which should give a very clean cut through plywood but still work on 2x4s and trim boards.  While I was there I checked their selection of driver bits again.  I was looking for a 3″ long No. 1 SR (square recessed) bit but they did not have any that long.  I found a 2″ bit for $2.48 but then I spotted a pack of seven 2″ long bits for under $4.  It had two #1, three #2 (the most common size), and two #3 bits from the same manufacturer as the single bit.  Can someone explain that pricing structure to me?  Apparently most of the cost is retail packaging.

Linda prepared large, wonderful salads for dinner.  She made her own dressing using balsamic vinegar, walnuts, raisins, garlic, and seasonings, and it was very good.  We finished the Pinot Grigio with the meal and then resumed our work.

I changed the blade on my saw and then we moved the wood and 2×4 supports back out into the driveway.  The new blade made very clean cuts confirming that changing it was long overdue.  The third piece of the alcove base was not as wide as the first two, measuring 28.25″ across the front and 28″ across the back.  (The alcove tapers in 1/4″ from front to rear along the right side.)  The depth was 26.75″ to match the refrigerator base depth, and a half inch deeper than the second piece.  I set it in place, snug to the right side of the alcove and flush with the front edge of the other two pieces, and checked for an even reveal along the left side of 5.75″.  Everything looked good so I screwed it down.

There are several reasons for this design/construction.  First, there is a large bundle of wires and two air lines that run across the floor of the alcove at the rear wall.  Using three layers of plywood allowed the top layer to be high enough for the base of the refrigerator to extend over the wire bundle and have its back about 1″ from the back wall (thus the reason for the recessed electrical outlet).  It will also leave about 1″ of clearance above the fridge, which is enough.  The second reason is that the 5.75″ width at the left, with only two pieces of plywood under it, is where the pull-out pantry will go.  But third, I will install a 24″ long 2″ x 2″ angle (steel or aluminum) on the middle sheet against the left edge of the top sheet to prevent the refrigerator from shifting to the left.  The front edges of the plywood base pieces will be covered (eventually) by a something, probably a piece of 3/4″ thick walnut hardwood, that will stick up above the top surface of the top piece just enough to keep the fridge from rolling out.  That piece, however, will have to be removable so I am still thinking about just how I want to secure the refrigerator case in the alcove.

Linda does her Vanna White impersonation, highlighting how the new pull-out pantry will look when it is installed.  The pantry is in its extended position revealing the slides sections that will mount on the cabinet wall.  The refrigerator is out so we can work in the alcove.

Linda does her Vanna White impersonation, highlighting how the new pull-out pantry will look when it is installed. The pantry is in its extended position revealing the slides sections that will mount on the cabinet wall. The refrigerator is out so we can work in the alcove.

We still had some light but with the heavy cloud cover it was darker than usual in the coach for this time of day (6:30 PM).  We rigged up a piece of twine to hang the work light and turned on as many interior lights as we could.  We then carried the pull-out pantry from the library (in the house) to the bus.  We brought all of the slides in as well, along with two pieces of 3/4″ plywood and a 4′ length of 2×4.

We set the two pieces of 3/4″ plywood in front of the left edge of the alcove flush with the two bottom base pieces.  We then set the 2×4 on flat (3.5″ side down) spanning the plywood inside and outside the alcove.  We installed the cabinet halves of the nine slides onto the pieces attached to the pantry and then set the unit in place with the bottom resting on the 2×4.  We moved the pantry in and out checking its position and considering where the slides needed to be attached to the alcove wall and exactly how we would do that so the front has an even reveal relative to the vertical front trim of the left alcove wall.

By this point it was after 8 PM, it was getting dark, and we were too tired to start something as critical as attaching the slides to the alcove wall.  We are behind schedule, but had enough sense to not push beyond our limits.  We closed up the bus, relaxed on the couch for a bit with our kitty cats, took some Advil PM, and went to bed at 9 PM.

 

2015/08/24 (M) Skimcoating

For a change of pace we had granola with vegan yogurt for breakfast.  I made seven cups of the Cafe Europe / Columbian decaf blend but Linda only had one mug as she was meeting Diane at Kensington Metropark at 9 AM to walk.  After she left I gathered up the laundry, sorted it, and started the first load.  I then turned my attention to the bus.

My first task was to cut one of the 8″x8″ sheets of #80 sandpaper in half, put it on the orbital pad sander, and go over all of the Universal Patch and Skimcoat (UPS) that I applied yesterday.  The 80 grit worked well and I only needed the one half sheet.  I swept the floor clean of loose debris and then assembled my tools and materials to patch a few gouges I missed yesterday and then skimcoat the entire portion of the floor that used to have ceramic tile on it.  I mixed 24 ounces (by volume) with 12 ounces of water (by volume), half as much UPS as I did yesterday.  I tried to work more quickly and got most of it applied.  I cleaned up my tools and let them dry while the compound cured.  That also gave me an opportunity to move laundry from the washer to the dryer and start another load in the washing machine.

I had a call from Chuck so I took a break to chat with him.  He and Barbara spent the weekend racing at the old Air Force base in Oscoda, Michigan.  Their bus and race car both ran well and he turned in some very good times.  He had installed a new turbo boost gauge in the bus and based on my experience had selected a 0 to 15, PSI VDO unit.  Apparently 15 PSI is not high enough for his engine.  I have seen the boost on my gauge, which is a 0 to 30 PSI model, go as high as 17, but not often.  For most of our trip to Arizona and back this past winter it did not go over 15 PSI.

The only issue they have with their coach at the moment is their old Amana residential refrigerator.  The freezer is apparently not keeping things as cold as it should and the ice maker is not working.  They use a lot of ice and generally have the freezer stocked, so those are problems.  They bought a bag of ice for the weekend but it appeared to get warm enough to develop surface moisture and then refroze into large chunks, inconvenient at best.  I think they have decided to replace it and want to do so before they leave for the winter and while they still have the shop and the forklift.

Chuck is also going to contact the glass installer and see if he would be willing to install bus windshields.  Both of his lower windshields need to be replaced as do both of ours.  We have five replacements at his shop, two for him and three for me.  I also have new gaskets but he needs to get two sets.  We discussed late September as the best time for me and he will see if the windshield guy will do all four of them on the same day.

I mixed the remaining USP, about 12 ounces (by volume) with 6 ounces of water (by volume) and finished the skimcoating of the bus floor.  I used the last little bit of compound to patch some screw holes and small gouges in the living room floor where carpet had been installed.  There may be a few more but instead of opening another bag of UPS I will probably return it and buy a quart of the premixed compound.  I then cleaned up my tools again and left them in the sun to dry.

Linda got home about this time.  It was just after noon, so we had a light lunch of vegan deli slices with lettuce, onion, and Daiya non-dairy cheese, on thin buns.  A pluot provided a nice, sweet finish to lunch.

We measured for wallpaper the other day so I took the notes and created an Excel spreadsheet to figure out how many rolls of wallpaper to order.  While I did that Linda worked on cleaning and reconditioning drawer fronts with Touch of Oranges and Touch of Beeswax.  After examining the wallpaper in the bathroom (of the bus) I think we need to replace it too.  We took a few minutes to get those measurements and I added them to the spreadsheet.

The wallpaper we have selected is the Lamar (#699-3377R) from the Just Textures collection of Sellars and Josephson.  It is an off-white color with a small texture pattern designed for reverse hang, random match installation.  It is only sold in 2-roll bolts 27″ wide and 4.5 yards long.  We will need more than six rolls to replace all of the wallpaper so we will have to order eight rolls even though we may defer doing part of the hallway and the bathroom for a while.  Fortunately it is not too expensive (as wallpapers go) and is scrubable, which was one of our requirements for use in the bus.  Linda will return the sample books to Delux Drapery and Shade Company in Ann Arbor on Wednesday morning and place the order.

Linda reheated the leftover fajita veggies from last night and fixed some white rice to go with them.  We had fresh strawberries and a little Coconut Bliss non-dairy ice cream for dessert.  Coconut Bliss ice creams are not too coconuty, and are appropriately named.  They are as good as I remember Hagan-Daas being.

I took a little time to add lines to my floor tile layout drawing showing the location of the underlayment sheets.  It looks like I may need at least eight sheets.  I have four sheets in the garage and will install those before buying more.  I spent the rest of the evening working on the article for Bus Conversion Magazine about Larry and Carol Hall’s GM4106 bus conversion and finished it around 10 PM.  I spent another 1.5 hours catching up on e-mail and checking in on the status of Technomadia’s bus renovation project at MasterTech in Elkhart, Indiana.  The weather has turned cool and should be perfect for working on the bus tomorrow.  We need to have long, productive days, so I had a snack and got to bed at midnight, played a few games, and went to sleep.

 

2015/08/22 (S) Clean and Level

We arrived at the SLAARC breakfast just before 8 AM.  We took the last two seats at the end of the long row of tables, but had to add another one as six more people came in after us.  We had a lively chat that lasted until almost 9:30.  After breakfast we stopped at the Tractor Supply Company store in New Hudson to get a couple more deer blocks and then headed for home.

We took a few minutes to put away tools and straighten up the garage enough that we could set up a work surface for Linda to use for cleaning the walnut drawer fronts for all of the bus drawers.  We set up the two sawhorses we got at Lowe’s yesterday, set two 8-foot 2x4s in the provided grooves, and set a 4’x8′ piece of 2″ rigid foam insulation across them to use as the work surface.  I found an old package of 4/0 steel wool and Linda found some old terry cloth towels.

Foam insulation work surface in garage with walnut drawer fronts laid out for cleaning with Touch of Oranges.

Foam insulation work surface in garage with walnut drawer fronts laid out for cleaning with Touch of Oranges.

Linda removed the drawer fronts from seven of the drawer boxes and tagged them so they could be reunited later as each front is uniquely paired with its box.  She then removed the handles from the drawer fronts and set them aside as they will be replaced with new ones once the cleaning is done.  She started with the back sides of the drawer fronts.  Following the directions she sprayed them liberally with Touch of Oranges wood cleaner, let them sit for 10 minutes, sprayed them again lightly, and rubbed them with the 4/0 steel wool.  She then wiped them off with a terry cloth towel and applied Touch of Beeswax using 4/0 steel wool, always working with the grain, of course.  The wax will have at least 24 hours to soak in before being wiped off.  Once that is done she will flip them over and repeat the process on the front side.

While Linda was doing all of that I hauled the 15 gallon DeWalt portable air compressor out by the bus, plugged it in, and connected the air hose.  I used the 4″ circular pneumatic sander on a few remaining high spots and decided I was done with it.  I had found some old packs of 80 grit half sheets and tried using them on my orbital sander but the grit disappeared very quickly and the sheets snagged and tore on splinters in the plywood.  I spent more time changing sheets than I did sanding with them so I abandoned this approach after the fifth sheet.  I did, however, find a half dozen splintered areas and prepared those by making stop cuts with a utility knife and then peeling the splinter free with a putty knife, creating voids that will be filled with leveling compound.

I was tired of sanding and was clearly not going to get the floor back down to bare wood.  I decided that the floor was as sanded and smooth as it was going to get and it was time to move to the next process; patching and leveling.  Before I could do that, however, I needed to clean the coach.  I vacuumed the floor three times and vacuumed all of the woodwork and wallpaper.  As I worked from the bedroom forward Linda followed behind with a microfiber cloth wiping down all of the woodwork.

I assembled the tools I needed to apply the Universal Patch and Skimcoat; a 3″ putty knife, a 5″ putty knife, a combination smooth and toothed rectangular trowel, a mixing bucket, and a 2 foot long wooden stir stick and a mixing paddle designed to go in a drill.  Each bag of UPS weighs 7 pounds and gets mixed with 1.75 quarts of water, which works out to 1 part water to 2 parts UPS.

The directions on the bag indicated that a full bag of UPS, properly mixed, would cover 20 to 25 square feet 1/8″ thick.  That’s only a 5’x5′ area, but I only had a few gouges that were 1/8″ deep, so an entire bag was going to cover a lot more than 25 square feet when applied as a skim coat.  Not having worked with this material before I had no idea how much working time I would have so I decided to mix half a bag.  The recommended mixing method using a paddle in an electric drill turned out to be a bad idea so used the 2-foot long wooden stir stick to mix the compound.

TEC Universal Patch and Skimcoat applied to the floor in that hallway.

TEC Universal Patch and Skimcoat applied to the floor in that hallway.

I started in the bathroom patching small depressions and then working out from the baseboards.  By the time I got out into the hallway I had not even used half the compound and it was starting to set up.  I hurried to use as much of it as I could, and tried adding a little extra water to extend its workability, but was only able to use about 60% of it before it was too stiff to spread and trowel off smoothly.  I could have waited 1 hour and then mixed and applied more compound but I did not want to risk disturbing what I had already done and it has to set for 24 hours before I can sand it, which I will have to do.

Cleanup required warm soapy water for the tools.  I then poured it into the 5 gallon compound bucket, topped it up with water, stirred it to dissolve the compound as much as possible, and let it sit.

For dinner Linda made Farro with mushrooms, onions garlic, glazed snow peas, and grated carrots.  She needed some dry white wine for the Farro dish and opened a bottle of Pinot Grigio, so we had a glass with the meal.  As rule if a wine is used in a dish it is also a good choice to drink with that meal.

After dinner I went to Lowe’s and got some more 4/0 steel wool and some 80 grit sandpaper sheets.  I stopped at O’Reilly’s for a battery disconnect switch for the lawn tractor but they did not have one.  I tried the Howell Tractor Supply Company but they did not have one either.  I drove to the Brighton Shell station, topped off the fuel in the Element, and went home.  We turned in at 9 PM and watched a 007 movie before going to sleep.