Tag Archives: CMI (Ohio)

2015/09/25 (F) Miss Dig

I turned the lights out at 11 PM last night and slept until 8:15 AM this morning.  I was preparing coffee when Linda told me there were wild turkeys in the back yard.  They were gathered at the deer feed block and more showed up while we were watching.  There were 15 in all, and they were big.  We had our usual granola for breakfast with fresh blueberries, strawberries, and bananas.  We finished our morning routine and coffee at 10 AM and got back to work on the bus.

Linda continued working on removing the old wallpaper while I worked on the entry and cockpit.  She used a drywall sanding sponge to try and remove the last little bit of material from the walls she stripped yesterday and it worked rather well but not 100%.  I was able to remove the step well cover assembly yesterday and today I removed the last step before reaching the main floor.  It did not come out easily; the three screws securing it to two adjacent walls were badly rusted and the Philips heads would not hold the screwdriver bit.  I ended up prying them loose, and inelegant (brute force) but effective solution.  I am going to rebuild this step with a slightly deeper run and an open front so we can store shoes under it.  First, however, I have to tile the floor.

I spent some time examining the old tile in the driver’s part of the cockpit.  It clearly goes under the accelerator pedal but around the brake pedal.  That’s reasonable as the accelerator is electrical, with only a cable that goes through a small hole in the floor, while the brake is pneumatic and the major part of it is in the bay below the floor with all of the air lines connected to it.  I came to the conclusion that the tile was also installed under the seat base, which means Creative Mobile Interiors removed the base to install the tile.  I did not come to a final decision regarding removing the tile versus tiling over it, but I am leaning towards removing it.

I was also able to determine that the retaining nut on the swivel bases for the pilot and copilot seats was 15/16″ and accessible from the rear with the seats moved forward.  That means I can remove the seat, 6-way power base, and swivel plate as one assembly by removing one nut.  I will then have excellent access to the pedestal mounting bolts and the driver’s area once everything else is out of the way.

Rebecca from Shutz HVAC called at 10:30 AM and arrived about 15 minutes later.  Shutz is the HVAC installation contractor for the Lowe’s in Howell and she was here to look at our main air-conditioning system and give us a quote on a new Trane system as that is what Lowe’s sells.  Lowe’s had a Pro Show on Wednesday and Rebecca was staffing the Shutz table so we stopped to chat.  She let us know that everything at Lowe’s was on sale through tomorrow at closing for 10% off with our Lowe’s credit card, including installation labor.  The card is automatically good for 5% off on any product purchase so the extra 5% is not enough of an incentive to cause us to make the purchase, but we were curious what a new system might cost.  I will get a quote from Darryl at DCM, however, before making any decisions.  Also, our friend Mike (W8XH) recently had an A-C system installed and was very happy with the company, product, and installation so I will find out who he used and get a quote from them too.

Rebecca was very nice and very knowledgable.  After looking at the condenser/compressor outside I got a step ladder and she went up in the attic to look at the old air-handler/evaporator.  The system is a Coleman and we have no idea how old it is; we just know that it did not do a good job of cooling the house this summer.  The quote was for a “3 ton” system for $7,800.  With 10% off it came to $7,020 but that price was based on flushing, testing, and reusing the existing refrigerant lines, which did not sound like a good idea to me.

Charles from USIC (Miss Dig) showed up around 11:30 AM to mark the utilities.  Phil plans to start digging and grading next week, hopefully Tuesday.  Charles came to the front door and I excused myself from the air-conditioning conversation to walk the property with him.  I explained what we were having done and showed him where the work would take place.  He marked the main gas line along the entire length of our property, a portion of the branch line going to our meter, the tie in for the branch line to the house across the street, and the T at the northwest corner of our property where the main line splits to service the court.  He also marked the phone line, which runs underground from a pole west of our house to the southwest corner of our garage.  The main electrical service runs underground with the phone line but someone else has to come out and mark that.  I chatted with Charles briefly before he left and then called Phil and left him a message.

Last summer Darryl from DCM Heating and Cooling installed a new natural gas furnace with an air conditioner for our library, a natural gas heater in our garage, ran all of the black iron pipe, including 160 feet of 2″ line, hooked us up to the gas meter, and got everything working for just under $11,000.  The Trane system would be bigger than the one for the library, and the air-handler in the attic is a more difficult installation, but $7,800 for just the air-conditioner without new refrigerant lines seemed a bit high.  After Rebecca left I called and left a message for Darryl.

Linda was ready to strip the wallpaper behind the built-in sofa so we moved the two desk pedestals onto a blanket on the kitchen floor in the bus and unscrewed the seat and set it on top of the desk pedestals.  When I finally got back to work on the bus I removed the cover for the front OTR HVAC system and set it aside.  I was trying to get access to the underside of the wood trim that includes a grab handle that needs to be tightened but had a look around first.

I noticed a damper controlled by a flexible cable and figured it was what determined if the air was fresh or recirculated.  I turned the knob on the dashboard and saw the cable move but not the damper.  The damper was stuck so I loosened it by hand but the knob still did not cause it to move.  I then noticed that the sheath of the flexible cable had come loose from its retaining clip.  It was a tight spot in which to work but I was able to loosen the two screws holding the clip using a right angle screwdriver.  I slipped the sheath under the clip, tightened the screws enough to hold it, and turned the knob.  It worked!  On a day when I did not feel like I was accomplishing very much this was a tangible and unexpected success.

I removed the only four visible screws from the wood trim but it would not budge.  I had tried removing it once before without success but was determined to get it loose this time.  The only reasonable explanation was that CMI had glued it on after tightening the grab handle as part of the initial work we had them do right after we bought the coach.  I carefully worked a pry bar under the passenger side end and gradually applied force to it.  It was, indeed, “glued” on but it appeared that I would be able to pry it loose without breaking anything if I took my time.

When I did finally get it off I could see that they had used clear silicon (adhesive) caulk to attach it to a dark gray plastic piece.  Royale Coach had originally attached it to this plastic piece using four screws.  The plastic piece turned out to be the lower windshield defroster duct and I am considering how we might finish this without replacing the wood trim.  Wallpaper is currently at the top of my list but I doubt that it would be a good solution.  Of further interest to us was the wood itself.  We presumed it was maple based on the color but were puzzled why they would have used a different wood in the entryway.  Once we saw the back side, however, it was obviously walnut that lightened where it was exposed to light to the point of looking like maple.  There is other wood in the entry and copilot area that is equally light and we now realized that we had a refinishing task and not just a cleaning task, ahead of us at some point.

My next task was to scrape as much of the caulk off as I could.  I got a lot of it off, but not all.  Silicon caulk is difficult to remove.  I eventually found a single edge razor blade holder and blade and used that to get the last bit off.  I then worked on removing layers of masking tape from the edges of the base where the former step well slide was installed.

I have some carpentry to do to rebuild the steps and prep them for the tile installation and needed some materials and supplies so I went to Lowe’s and got:

  • Adhesive remover;
  • A 4’x8′ sheet of 3/16″ SurePly underlayment;
  • Two 3/4″ x 2.5″ – 6′ poplar boards;
  • A 15/16″ open or closed end ratcheting wrench;
  • A bottle of Piranha Wallpaper remover;
  • A Piranha wallpaper remover sponge;
  • A pack of 2,000 18 gauge 3/4″ long x 1/4″ crown staples;
  • A pack of 25 sheets of 120 grit and a pack of 25 sheets of 220 grit 1/4 sheet sandpaper.

I got 10% off the total bill! which was nice.  I did not get a palm sander as they were out of the Porter Cable model I wanted.  The Lowe’s in New Hudson showed two in their inventory so we will stop there tomorrow after breakfast and get one.  I also needed a half sheet of 3/4″ plywood to make a new platform to replace the step well slide but did not feel like dealing with that.

For dinner Linda heated some butternut squash ravioli she bought at Whole Foods.  She served it with sliced vegan Italian sausage cooked with mushrooms, onions, and garlic, a side dish of steamed fresh green beans, and a glass of Moscato.

After dinner I uploaded my blog posts for July 23 through 31 plus a gallery post of 11 photos I got from Jarel Beatty of the custom walnut desk in the process of being built in his shop.  I got a call back from Darryl and we discussed the new air-conditioning system.  He said he would get me a price but advised us not to let anyone reuse the old refrigerant lines.  If they are not 100% clean the old refrigerant will contaminate the new system.  If Shutz installs the Trane system it comes with a 10 year parts and labor warranty, but it would still be a hassle to deal with getting a contaminated unit repaired or replaced.

After chatting with Darryl for a while we agreed that there wasn’t any urgency to this.  For one, we need to have Darryl check the current system for leaks, and assuming it does not have one, for proper refrigerant charge, cooling capacity, and airflow.  Darryl is busy doing heating systems at the moment, but is willing to do the maintenance work.  Also, the cooling season is done for this year and we will be traveling during the hottest part of next summer.  A final factor is that this has been another expensive summer for us with the new roof on the house, the interior remodeling of our motorcoach, and the work Phil is about to do, so we would prefer to defer this expense.

 

2015/09/16 (W) CSD to GLCC

I spent the night in the coach at Coach Supply Direct, in the fenced in parking lot, next to the train tracks that run parallel to M-62 through Edwardsburg, Michigan.  I was up late and went to bed tired.  The trains did not bother me (they run at every hour of the day and night) but aching knees and joints in my hands, especially the base of my thumbs, made for a less than sound sleep.  I had also not leveled the coach when I arrived yesterday but it was slightly low to the front passenger side so it did not bother me as me head was higher than my feet, the head of the bed being on the driver’s side of the bedroom.

I had granola for breakfast, checked my e-mail, and was just settling in to start today’s post using my iPad when Josh showed up at 7:30 AM.  He opened the building and retrieved a small desk/cabinet and loaded it into his car to take back to the cabinet maker.  A portion of the back needed to be finished as it will be exposed when installed.  Having just been through the process of designing built-in RV furniture and interacting with a cabinet maker I understood how a detail like this could easily be missed.  We were fortunate in our choice of Jarel Beatty, as recommended by our friend Butch Williams, to build our pieces.  Jarel’s meticulous attention to the details of how something would be constructed, installed, viewed, and used, resulted in our not having any post-construction issues.

After Josh left I checked the status of the house batteries.  They were at 81% SOC (State Of Charge). Not bad after 11 hours of use.  Extrapolating, it appears that given some reasonable energy management we could go 24 hours without recharging before hitting the 50% SOC level.  I did not, for instance, use the microwave oven.  That is much better than before we replaced the refrigerator so it appears that the new one is clearly more energy efficient than the old one.

I also checked the coolant levels in the Aqua-Hot and generator expansion tanks.  The Aqua-Hot tank was still above max cold but the unit was also still a bit warm to the touch.  The level in the generator tank yesterday was very low with the engine fully warmed up and operating under load so I added antifreeze up to the “hot” mark.  If was slightly above that level this morning although I expected it to be lower as the system cooled off and drew the coolant back in.

Tyler showed up at 8:15 AM and knocked on the door.  He had stopped at McDonald’s and bought me a large coffee, half regular half decaf.  He had asked about this before leaving yesterday and remembered it this morning.  I was impressed with both his memory and thoughtfulness.  He got right to work on the cockpit seats, starting with the driver’s seat.  Before installing it, however, I had him repair the swivel plate.

That plate has always wobbled which was an uncomfortable and annoying sensation while driving.  Now that I had a clear view of the top of the plate it was “obvious” that there was once a washer under the retaining nut but it was no longer there.  Tyler removed the retaining nut, found a large washer with the correct hole size, put it on the threaded shaft, replaced the retaining nut, and tightened it.  No more wobble.

I am always trying to deconstruct the details of how this coach was built or serviced.  My best guess is that old seat was removed when CMI installed the tile floor in the cockpit area right after we bought the bus.  The installer probably removed the seat from the swivel plate in order to have better access to the pedestal and the area around it to lay the tile and either did not replace the washer or failed to recognize that it was missing and needed to be replaced.  I will never know for sure, but that’s my best guess.

Tyler bolts the new Flexsteel driver’s seat to the existing pedestal swivel base.  There is not a lot of room to work around the base of this seat.

Tyler bolts the new Flexsteel driver’s seat to the existing pedestal swivel base. There is not a lot of room to work around the base of this seat.

I connected the chassis batteries so Tyler could connect the 12V DC power to the seat and reposition it.  The outside rear mounting bolt was particularly difficult to reach but with the power on he was able to slide the seat forward and swivel the front to the left creating better access to the left rear.  Once it was bolted down he had me sit in it and make sure all of the adjustments worked.  They did!  The seat is comfortable, fits better in the available space, and has a range of adjustment that should allow either of us to position it comfortably.  It is still a little tight on the left side, but not like the old chair, and the only control there is a manual level for adjusting the back tilt that I can reach it without difficulty and generally do not change once I have it adjusted.

When Josh returned at 10 AM with the parts for the living room slider bases he and Tyler got busy prepping them.  Linda texted me around 10:20 for a status update and I suggested that she not leave before 1 PM.  There was more custom work required to get the chairs assembled and mounted than I thought there would be, but as I was able to watch every step of the process, and talk to Josh and Tyler as they worked, I could clearly see what the problems were and what they were doing to solve them.  They were on task and focused on getting it done correctly.

One of the new Flexsteel 529 captain’ chairs with the new swivel/slide pedestal base attached.  Note the handle for the swivel release.

One of the new Flexsteel 529 captain’ chairs with the new swivel/slide pedestal base attached. Note the handle for the swivel release.

The problem this morning was getting the swivel release cables on the cockpit seats to stay in place when the swivel tang was released from the detent in the base.  The reason for the problem is that we are reusing the old swivel bases because they have base plates that match the mounting bolt locations in the floor.  The way the swivel release cable is retained on these bases, however, is different from the attachments on the ends of the new cables.  Tyler was able to figure out a solution but it took a little time.  I don’t mind paying for that kind of experience and problem-solving.

I texted Jarel to give him a status update and indicated that we could come down Thursday, Friday, or Saturday to pick stuff up.  He texted back that any of those days would work.  I checked the Magnum remote and the SOC status had gone back to “Think’n”.  Nuts.  This has happened before with the Battery Monitor Kit and I think it has to do with the 4-pin connector that plugs into the bottom of it.  Whatever the case I need to investigate and fix it if I can.

The two class C captain’s chairs installed on the passenger side of the living room.

The two class C captain’s chairs installed on the passenger side of the living room.

With the driver’s seat installed I sat and tested its various adjustments and found a position that I liked.  Next came the two class C captain’s chairs for the passenger side of the living room.  Tyler and I worked for quite a while using a base with no chair on it to determine the correct location for the bases.  The seats needed to be far enough from the passenger side wall, the desk, and the co-pilot seat to swivel without interference but no farther as we did not want them to encroach into the center isle one inch more than necessary.  We also ran them through their full range of slide and swivel motions to make sure we could pull them up to the table.

We ended up with the edge of the front seat 16″ from the front edge of the main floor and 16″ from the HVAC duct.  We checked it for square and marked the holes.  Tyler drilled pilot holes using nuts to limit the depth.  We set the chair in position and secured it with four lag screws.  We measured 36.5″ to the front edge of the second base and positioned the base 16″ from the HVAC duct.  We made sure it looked right and then Tyler marked the hole locations and we removed the temporary base.  He drilled the pilot holes, we set the chair in place, and lag screwed them into floor.

The new navigator (L) and pilot (R) seats installed in the cockpit.  The navigator seat has a powered footrest.  We reused the old 6-way power bases for both seats.

The new navigator (L) and pilot (R) seats installed in the cockpit. The navigator seat has a powered footrest. We reused the old 6-way power bases for both seats.

With the captain’s chairs installed in the living room Tyler installed the co-pilot seat.  Once that was done the job was finished except for the cleanup and paperwork.  Josh and I chatted some more about the Corian desk top.  He had inquiries out to three suppliers but was having trouble getting replies from them.  We needed a temporary desk surface, so Tyler cleaned off the 4’x8′ piece of 1/2″ plywood that had served as the workbench for integrating the seating components. He marked and cut a 72″ long x 24.5″ deep piece.  I notched the center of the back edge 18″ wide by 3″ deep.  Tyler and I installed it while Josh totaled up the bill.  I wrote him a check for the balance due, prepared the coach for departure, and left a little after 2 PM.

I could have titled this post “Edwardsburg to Elkhart” but I like to keep my titles short.  The trip from Coach Supply Direct in Edwardsburg, Michigan to Elkhart Campground in Elkhart, Indiana was a short trip of approximately 15 miles that took about 25 minutes.  Upon arrival I parked the coach to the side of the entrance road and went in to the office to register.

We have been to this campground many times before but I managed to miss the turn for the row with our assigned site so I had to go all the way around a second time.  Once I had the bus in the site I leveled it and then shut it down.  I texted Linda our site number and then chatted with other GLCC chapter members who were already there and parked.

While I helped set up tables in the meeting room Linda arrived and got the cats, litter tray, etc. on board our coach.  After settling in for a few minutes I called Terry at A-1 Upholstery.  She was there so we drove over to pick up the sofa cushions, wrote her a check for the balance, and drove back to camp.  We were unloading the cushions when Dan stopped by.  He had retired at the end of July and bought a converted GM4104 a couple of weeks later.  His wife Kathy and son James had made the trip up from Huntsville, Alabama just for this rally.  They planned to join FMCA and GLCC but wanted to check us out first.

Linda had cleared the sofa earlier and put stuff away under the bed.  By the time I came in she had the new sofa cushions in place.  They were a tight fit but they looked nice.  We might make a small adjustment to the depth of the plywood seat but I think they are going to work out OK.

Linda went to the meeting room to help prep dinner and heat our vegan chili.  I took a short nap and joined her at 6 PM to eat.  We went back to the coach and gave Ed Roelle the tour and chatted for a while.  We then went back to the club house, met up with Vickie, and went for a walk.  When we got back to our coach I opened the box of Franzia Moscato and poured two glasses of wine.  We took two lawn chairs over to Scott and Tami’s bus to sit and chat.  Scott Crosby of www.busgreasemonkey.com was also there.  He arrived after I did in his 1948 GM 3751 “Silverside” bus.  It eventually got chilly so we went inside and went to bed where I worked on blog posts for a while on my iPad.

 

2015/05/28 (R) Ice Cold Internet

I was up until after 1 AM last night fussing with my computer but the OS was updated and was running better (I think) when I finally went to bed.  I need my beauty rest so I did not get up until 9 AM this morning.  Linda had already made coffee so I checked the temperature of the refrigerator (41.4 degrees F) and then got out the soy creamer.  41 is better than 45 but given where the thermostat was set the temperature in the fresh food compartment should have been 35 degrees or lower.  We had a very late breakfast of homemade granola and small glasses of orange juice to wash down our vitamins.

Because I did not get to upload any blog posts last night I switched up my routine and spent the morning working at my desk.  The weather was very nice so Linda went for a long walk.  My computer was back to normal and I managed to upload nine posts to my blog (May 10 through 18) by 1 PM.

I had an e-mail back from Ken Schramm yesterday letting me know that his “last day at Wayne RESA” gathering would get underway around 3:30 PM at Ashley’s Beer & a Grill at Westland Mall.  Brendan and Shawna’s celebration is from 5 to 8 PM in Ann Arbor so we will be able to attend both events although we might not make it to Ann Arbor until 6 PM.

Today was our friends’ 44th wedding anniversary.  Butch and Fonda were married the same year we were one day before us.  We did not know each other then but are now friends through our mutual passion for converted highway buses.

Brendan called and talked to Linda.  It turns out that tomorrow is grandparents/special friends Shabbat at Madeline’s daycare center and Brendan thought we might want to attend.  It starts at 10:30 AM and includes lunch.  The food at the daycare center is vegetarian but not vegan so we will see how that works out.  Brendan is going to take care of Linda’s plants so we will take these with us and go to his house when we are done at the daycare center.  I will pick up our electric pressure washer while we are there so I can wash the bus on Saturday.  We were going to buy cards today for Ken, Brendan, and Shawna but decided we would do that tomorrow on our way to Ken’s gathering.

Linda made large green salads with chickpeas for lunch.  We both put on a few pounds over the winter and really want/need to take them off.  After lunch I worked in the bus.  I removed the wood trim along the top of the beveled strip mirrors on the wall in hallway.  The strips were glued directly to the wall so I put the trim back on.  If we do not want to see these mirrors we will have to figure out some way to cover them.

There was a triangular horizontal panel between the upper edges of the J-lounge and the dinette with four switches mounted in it.  Two of those switches no longer control anything but the other two still do.  I secured the panel above the passenger side HVAC chase and blocked it in so it could not move.  I dressed all of the loose wires with cable ties and cable clamps and secured them to the floor.  I cut two grates from a piece of expanded metal and secured them over the two holes in the driver side HVAC chase where the sleeper-sofa was installed.  That sealed up the last of the holes that the cats might get into.  If one of them got into the HVAC system we would have disassemble half the bus to get them out.

I removed all of my tools and miscellaneous parts from the bus and set them on steps leading to the house.  I had put one of our folding chairs inside the bus to sit on and moved it to the location of the passenger chair as a safety barrier after I moved the trash can out yesterday.  I folded it up and put it back in the bay where it is stored.  While Linda vacuumed the inside of the coach with our Shop-Vac I put tools and parts in the garage or back into the appropriate tool boxes.  When she was done we got the Shop-Vac out of the bus and put it in the garage.

There is a maple grab handle on the right side of the entrance stairs (as you enter the bus) attached to a piece of maple trim from the back side.  The finish is worn and the handle is loose.  I wanted to tighten it, which required access to the back of the trim board.  Linda recalled that we had Creative Mobile Interiors (CMI) tighten this handle when we first got the coach so we figured there had to be a way to get to the back of the trim board.

We removed the cockpit HVAC access panel just below the trim board but it did not appear to provide access to the back of the trim board.  I removed the only two screws I could see (at the right end of the trim) but it still would not come loose.  I figured the trim board had to be screwed on somewhere else and the only possible place was under a piece of inset brass finish trim.  This brass trim is used throughout the bus, including around the edges of the Corian counters, and has an adhesive backing.  I have found screws under it in other places so I pried the end up and peeled it out, revealing three screws.

I thought I was on the verge of success until I removed the three screws but still could not get the trim board loose.  I tried prying it at various points with a screwdriver but it would not budge and we finally came to the unhappy conclusion that it was glued on.  Perhaps it is secured from underneath in some manner that we did not see but I will have to return to this when I have more time.  Linda suggested that we cut the handle off and install a new one that can be screwed on from the front.  She’s a clever girl.  As long as the access panel was off we vacuumed out the cockpit HVAC system and then replaced the panel.

About this time a UPS truck went by headed deeper into our neighborhood.  Since we live on a dead end street I knew the truck would be coming back so I waited for it and flagged down the driver.  I explained to the young man that we had two packages delivered to the wrong house in the same week about a month ago and that I had called the 800 number and talked to customer service but I would appreciate it if he would mention it to his colleagues as we will be ordering a lot of stuff starting in the second week of June.  He was very nice and said he would.

Our last bus task for today was the hard one.  We moved the passenger chair from the garage back to the bus using a hand truck so we did not have to carry it.  It is very heavy but with Linda guiding the top and me supporting the base we got it inside and set in position.  We tilted it fore and aft so I could slide the mounting studs into position and line them up with the holes in the base.  I then bolted it down to the support rails by tightening the four nuts.

This was all trickier than it sounds.  The bolts have square flanges that have to engage in the open slot of the channel to keep them from turning while being tightened or loosened.  But that required me to pull up on the studs as the nuts were not going on that easily.  As when I took the nuts off, I had to wedge one of them up with a screwdriver while I got the nut tight enough that the bolt would not spin.  I reconnected the power to the chair and we checked that all of the adjustments still worked, especially the footrest.

With the installation of the passenger seat we were done working on the bus until after GLAMARAMA and have two seats with seatbelts so we can tow the car rather than drive it separately.  This will be much nicer for us and the cats, although I expect the modified interior will freak them out initially.  We will be gone most of Friday but have Saturday to prepare food, reload the coach for the week, and wash the exterior.  Oh the joys of owning a converted coach.

For dinner Linda served the last of the whole wheat capellini with Portobello mushrooms and asparagus and steamed some broccoli.  A piece of whole wheat bread and a small glass of Leelanau Cellars Winter White wine completed the meal.  We had watermelon for dessert later.

I returned to my office after dinner and updated our Rand-McNally RVND 7710 GPS.  I then continued uploading blog posts.  By the time I quit working around 10 PM I had uploaded nine more posts and was caught up!  I think 18 posts in one day may be my all time record.  I did not get to work on articles for BCM, or copy files between our NAS units, but I was satisfied with what we had accomplished today.