2015/11/10 (T) A Rainy Day

I checked the TV weather station before I turned off the lights last night.  Rain covered most of Indiana and Ohio and was moving northeast.  We were going to get clipped by the western edge of the moisture but the heaviest rain was forecast to pass to our south and east.

Linda planned to go into the bakery today and had her alarm set for 5:45 AM.  It went off and I woke her up enough to shut it off and go back to sleep.  Around 6 AM we both received e-mails on our iPads and phones, a sure sign that we had lost power to the house.  I was awake at this point but stayed in bed until 6:45.  I was not falling back asleep, so I put on my robe and made coffee.  I finished up the Kenya AA, which is not decaffeinated, figuring we could both use the boost this morning.

While the coffee was brewing I cleaned the cats’ litter tray and checked my e-mail.  I had a reply from Bill Tharpe which decided for me that I would be going to Indiana on Friday.  I also had replies from the two Mitch’s who had contacted me as about articles I wrote in Bus Conversion Magazine and replied to both of those.  I edited the e-mail with the minutes of Sunday’s SLAARC meeting and forwarded it on to the club officers.  An e-mail from Gary at BCM indicated that they still needed a photo of Byron and Betty Pigg for the December featured bus article, so I replied and cc:d Byron.  Writing for BCM is sometimes a lot of work, but it’s a hobby for and I enjoy it so I do not mind.

It was wet outside and still raining lightly, a perfect day to sit by the fireplace in a robe and drink hot coffee.  Phil was hoping to return today with a load of screened topsoil and get it placed and graded along the edges of the driveway but said it would depend on the weather.  Once the topsoil is taken care of he will grade the driveway with his bulldozer and make sure the 40 foot long parking area is as flat and level as possible.

Linda finally got up at 8:30 and was starting to get dressed to go to the bakery when I suggested she stay home, rest, and get well.  She was immediately OK with that idea, put on her robe, and took her iPad to the living room to enjoy the warmth of the fireplace and some hot coffee.  I finished up my draft blog post for yesterday, e-mailed it to myself, and started this one.  I really cannot afford to lose a whole day of work on the bus but this is the kind of day where we like to just sit and do quiet things, or even nothing at all.  We finally finished our coffee, got dressed, and had a light breakfast at 10 AM.

Taking care of Madeline for three days and nights took a lot of Linda’s mental and physical energy and her cold took what was left.  She headed back to bed and I got my thoughts organized relative to working in the bus.  I talked to Jarel yesterday and found out that it would cost $50 to have a sheet of 1/4″ Baltic Birch plywood delivered to his shop because he did not have a regular delivery scheduled and the $50 cost of the 60″x 60″ sheet would not meet the minimum cost for free delivery.  I did not need the piece of plywood badly enough to pay a 100% surcharge to get it so that idea was off the table until next year.

My goal for today was to get a piece of SurePly underlayment cut and installed on the passenger seat platform.  Before I even started on the piece I had to resolve what to do about the four carriage bolts that are used to mount the base.  One of the four bolts has some messed up threads but I have a tap and die set and might be able to clean them up.  However, I am adding the thickness of the underlayment and floor tile plus a washer to what was there before so I wanted to use a longer bolt.  I already knew that Lowe’s and O’Reilly’s did not have what I needed and I presumed that The Home Depot did not either.

I finally went to Howell Hardware and had a good QSO with Steve (N8AR) on the drive there.  As I had been told they had a very good selection of hardware, by the piece, but they did not have fine thread carriage bolts in the 1/2″ size I needed.  I bought four of the 2″ long coarse thread bolts, four flat washers, four lock washers, and four nuts.  I also picked up a large washer to match the other three I already had for securing the central mounting stud along with two nylon washers.  That trip took over an hour out of my day before I even got started on my main task.

It took me several hours and many trips back and forth between the bus and the shop (in the garage) to get the piece of underlayment to fit just right.  I made one small mistake but the piece was large enough and complicated enough that I did not want to take the time or material to remake it.  Before I could install it I needed to get the outside end of the floor patch secured.  Yesterday I tried to screw that end to the material underneath it but the screw would not penetrate.  I scratched my head for quite a while until it occurred to me that I could use a small angle bracket attached to the vertical wood wiring chase in the forward outside corner.  I had limited access to that area, and it took me multiple attempts before I finally got the screw in, but I did.  Securing the bracket to the floor patch was a lot easier.

After securing the end of the patch I realized that the area between the front mounting channel and vertical front of the platform was slightly concave.  It was not a big dip but it was big enough that it needed to be patched.  Floor patching compound was the last thing I wanted to deal with today but it turned out to be just that, because once I applied it it had to dry for hours.  It was heavily overcast all day and my mood was correspondingly suppressed so I felt like I was doing everything in slow motion.  Based on the fact that I did not even get the piece of underlayment installed perhaps I was.

I try to keep an eye on the “house” batteries in the bus.  When I checked them this afternoon the reported voltage was higher than normal so I turned off the charger function on the Magnum 4024 to let the batteries rest and see where the voltage really was.  The DC draws on the battery bank were minimal.

I am finishing this post a couple of days later and no longer recall what Linda fixed for dinner but whatever it was I’m sure it was good.  After dinner we relaxed in the living room for a while, watched our Tuesday evening TV programs on the larger TV set in the basement recreation room, and then went to bed.

 

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